米桑油田高压盐膏层固井问题分析和优化
投稿时间:2018-03-04  修订日期:2018-07-02  点此下载全文
引用本文:张晓广.米桑油田高压盐膏层固井问题分析和优化[J].钻探工程,2018,45(9):37-41.
ZHANG Xiao-guang. Analysis and Optimization of Cementing in High Pressure Salt-gypsum Layer of Missan Oilfield[J]. Drilling Engineering, 2018,45(9):37-41.
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作者单位E-mail
张晓广* 中海油能源发展股份有限公司工程技术分公司 zhangxg@cnooc.com.cn 
中文摘要:对米桑油田部分井出现的高压盐膏层井段固井质量差且影响下步作业的情况进行了分析,优化了前置液设计、水泥浆设计、入井套(尾)管现场检查、下套管前井眼要求、固井前井筒要求、套管居中、固井注替、固井质量检验等,并成功应用于47井高压盐膏层井段固井,为后续开发井类似井段的固井质量提升提供了借鉴。
中文关键词:高压盐膏层  固井  防窜  米桑油田
 
Analysis and Optimization of Cementing in High Pressure Salt-gypsum Layer of Missan Oilfield
Abstract:The poor cementing quality occurred in some high pressure salt-gypsum layer of Missan oilfield is analyzed together with the influence on the next operation are analyzed, the design of preflush and cement slurry, on-site inspection of casing and liner, borehole requirements before casing running, borehole requirements before cementing, casing eccentricity, cementing by mud grouting & displacing and cementing quality checking are successfully applied in the high pressure salt-gypsum sections of 47 well, which provides a reference for the cementing quality improvement in similar situation.
keywords:high pressure salt-gypsum layer  well cementing  channeling prevention  Missan oilfield
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