特深井大尺寸井眼Ø168.3 mm S135钻杆失效分析与对策
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作者单位:

1.川西钻探公司钻井技术研发中心,四川 成都 610051;2.中国石油集团川庆钻探工程有限公司,四川 成都 610051

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中图分类号:

TE921+.2;P634.4

基金项目:

中国石油天然气集团有限公司关键核心技术攻关项目“万米超深层油气资源钻完井关键技术与装备研究”(编号:2022ZG06)


Failure analysis and countermeasures of Ø168.3mm S135 drill pipe in large size hole of extra-deep well
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Affiliation:

1.Drilling Technology Research and Development Center of Chuanxi Drilling Company, Chengdu Sichuan 610051, China;2.CNPC Chuanqing Drilling Engineering Co., Ltd, Chengdu Sichuan 610051, China

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    摘要:

    为提升大尺寸井眼中钻具强度,某特深井首次采用?168.3 mmS135钻杆,有效保障了大尺寸井眼钻具安全,但回厂检测钻杆时仍然发现了多种失效形式。通过钻杆生命周期追溯、统计分析、钻柱力学分析以及实验研究等方法找到了失效原因。研究表明,大尺寸井眼中?168.3 mm钻杆失效类型主要是螺纹磨损、钻杆弯曲、钻杆腐蚀和疲劳失效。螺纹磨损主要是由钻杆使用时间长、上卸扣次数多引起,但常规API螺纹结构也有待优化以提高螺纹抗磨损能力;钻杆弯曲是由于钻杆在大拉伸载荷下,长时间承受较大弯曲应力最终导致其发生塑性变形;钻杆腐蚀是由于出井钻杆表面残留有钻井液,在空气-水-氯离子的环境中腐蚀速率大大增加;钻杆疲劳失效是由钻铤附近的钻杆应力集中明显、大尺寸井眼中钻具弯曲变形大引起。基于钻杆失效原因分析,提出了预防大尺寸井眼中?168.3 mm钻杆失效的措施。研究成果可为S135钢级?168.3 mm钻杆在特深井大尺寸井眼中的安全应用提供指导。

    Abstract:

    To improve the strength of the drill pipe in the large-size hole, the ?168.3mm S135 drill pipe was used for the first time in the extra-deep well, which effectively guarantees the safety of the drill pipe. However, various failure forms are still found in the drill pipe inspection. To study the failure causes of the ?168.3mm S135 drill pipe in the large-size hole, the failure causes were identified through tracing the life cycle of the drill pipe, statistical analysis, drill string mechanics analysis and experimental study. The research shows that the main failure types of ?168.3mm drill pipe in large hole are thread wear, drill pipe bending, drill pipe corrosion and fatigue failure. Thread wear is mainly caused by the long use time of drill pipe and repeated make-and-break operations. Besides, the conventional API thread structure also needs to be optimized to improve the thread resistance to wear. The bending of drill pipe is caused by the plastic deformation of drill pipe which is subjected to large bending stress for a long time under large tensile load. The corrosion of drill pipe is caused by the increase in corrosion rate in the environment of air-water-Cl- due to the residual drilling fluid on the surface of drill pipe. The fatigue failure of drill pipe is caused by the obvious stress concentration of drill pipe near drill collar and the large bending deformation of drill pipe in large hole. Based on the analysis of the failure causes of drill pipe, the measures to prevent the failure of ?168.3mm drill pipe in large hole are put forward. The research results can provide guidance for the safe application of S135 steel ?168.3mm drill pipe in extra-deep Wells with large size boreholes.

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蔡明杰,付强,贺明敏,等.特深井大尺寸井眼Ø168.3 mm S135钻杆失效分析与对策[J].钻探工程,2025,52(4):69-74.
CAI Mingjie, FU Qiang, HE Mingmin, et al. Failure analysis and countermeasures of Ø168.3mm S135 drill pipe in large size hole of extra-deep well[J]. Drilling Engineering, 2025,52(4):69-74.

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  • 收稿日期:2024-10-25
  • 最后修改日期:2025-02-21
  • 录用日期:2025-02-21
  • 在线发布日期: 2025-07-04
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