双聚防塌钻井液在北京某地热井中的应用研究
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1.自然资源部浅层地热能重点实验室,北京 100012;2.北京市地热调查研究所,北京 102218;3.北京探矿工程研究所,北京 100083;4.中国地质调查局绿色钻探技术创新中心,北京 100083

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TE254;P634.6

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Application research of bi-polymer anti-collapse drilling fluid in a geothermal well in Beijing
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1.Key Laboratory of Shallow Geothermal Energy, Ministry of Natural Resources, Beijing 100012, China;2.Beijing Geothermal Research Institute, Beijing 102218, China;3.Beijing Institute of Exploration Engineering, Beijing 100083, China;4.Technology Innovation Center of Green Drilling, China Geological Survey, Beijing 100083, China

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    摘要:

    北京市某地热井在钻探施工中遇到泥岩造浆严重、钻井液性能恶化、井壁坍塌、卡钻埋钻事故频发等诸多技术难题。针对该井存在的问题,本文系统阐述了原钻井液体系的改进方案及双聚防塌钻井液的工程应用情况。通过室内实验,对原钻井液的流变性、滤失量、抑制性等性能指标进行优化改进,并在钻探现场应用,实现原钻井液向双聚防塌钻井液体系的逐步转化。实践证明,改进后的钻井液在护壁效果、流变特性、润滑性能及钻进效率等方面均获得显著提升。研究同时指出当前钻井工艺中固控设备效能不足等局限性问题,并提出针对性技术建议,为同类地热井工程的钻井液设计与施工提供重要参考。

    Abstract:

    During the drilling construction of a geothermal well in Beijing, numerous technical challenges were encountered, including severe mud-making in mudstone, deterioration of drilling fluid performance, hole-wall collapse, and frequent occurrences of pipe sticking and burying accidents. Aiming at the above problems, this paper systematically expounds the improvement scheme of the original drilling fluid system and the engineering application of the bi-polymer anti-collapse drilling fluid. Through laboratory experiments, the performance indexes of the original drilling fluid such as rheological properties, filtration loss, and inhibition were optimized and improved, and the bi-polymer anti-collapse drilling fluid system was gradually transformed from the original drilling fluid and applied on field drilling. The practice has proved that the improved drilling fluid has achieved significant improvements in hole protection effect, rheological characteristics, lubrication performance, and drilling efficiency. The study also points out the limitation such as insufficient efficiency of solid control equipment in the current drilling technology and puts forward targeted technical suggestions, providing an important reference for the drilling fluid design and construction of the similar geothermal well projects.

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引用本文

孙振添,邹志飞,何铁柱,等.双聚防塌钻井液在北京某地热井中的应用研究[J].钻探工程,2025,52(4):121-128.
SUN Zhentian, ZOU Zhifei, HE Tiezhu, et al. Application research of bi-polymer anti-collapse drilling fluid in a geothermal well in Beijing[J]. Drilling Engineering, 2025,52(4):121-128.

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  • 收稿日期:2025-05-25
  • 最后修改日期:2025-06-10
  • 录用日期:2025-06-11
  • 在线发布日期: 2025-07-04
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